LOL, that is the part that I get attention with every time I load or unload. Obviously some long ramps. But the trick is the remote control for the golf cart. It's a Cricket Miniature Golf Cart. You can get that thing with a remote control option. Well spent money. I push a button and that thing...
I kinda miss the Maverick but I also don't. Coming from a Lariat First Addition with active cruise control and all that good stuff to an XLT Ranger was a step-down. But! That Ranger is more off-road capable than I could ever imagine. While boondocking in Utah and Wyoming we drove the Ranger into...
When we got the Maverick, there was no tow kit available yet. We transferred to 4 down in September of 2022. Roadmaster to be precise. It worked well for many miles. Well, until a dealership in Reno crashed the truck. We now tow a 2023 Ford Ranger. That thing got us into places, the Maverick...
I saw that when doing my research.
We will keep this one for a while. Took the rig over the scale not too long ago. 5000 Lb on the dot with the miniature golf cart in the bed. I am impressed by how off-road capable this truck is. It already got us into places the Maverick would have never gone...
Maybe I should write a final update.
As already written, we had a flat tow kit installed. At first, things worked well, but by June 2022 we started having issues with the 12-volt battery. I ended up disconnecting the Invisibreak system most of the time. In April the truck went dead on us. I...
Sorry, I am done with the Maverick.
The dealer is hoping that they don't total it. They are willing to give us 35k for it. And that's precisely what a new Ranger would cost us.
Plus! We are traveling and have to be in South Dacota for 4th of July. They will never have that repaired on time. New...
The last update.
After adding brake issues to the mix, and drooping it off at yet another dealership, Larry was crashed by one of the techs.They think it might be totaled. We should know more in the first week of June. We are moving on to a 4x4 Ranger.
Time for an update.
The truck sat at Borman Ford in Las Cruces, NM for a week without even looked at. My guy from Customer Experience Specialist/Dealer Experience Specialist, Ford CX/DX Team (short my Guy), arranged for a transfer to Viva Ford in El Paso, TX. Monday they were able to look at...
Anything is possible. But now I have the wiring diagram. All 2113 pages of it. :)
Will be digging into that tonight. For now, we are still on the road. Driving to Phoenix.
LOL, you can't make this easy can you?
Well, we will leave the truck behind and enjoy Phoenix and the Grand Canyon for the next two weeks. Hopefully, they figure it out here and don't take too long. Although I admit that I am itching to figure this out. As much as this is a pain in the rear end...
Darnon informed me that that's the power connection from the Underhood Junction Box to the Body Control Module.
Once you apply 12 volts to the cable, it drops to 3.6 volts. So, either some bad connection somewhere within the cable itself or ground or maybe a bad BCM.
It's definitely an...
I posted my NEW issue on another thread on this forum. The link is below. Basically the low voltage issue moved on to a different cable. I fixed the original harness issue with below pictured terminals. I also used a piece of copper plate to make the whole thing a little longer and take the...